Analysis and Solution of Folding Defects in Transmission Second Shaft Gear Forging

Folding represents a critical defect in gear forging manufacturing, occurring when oxidized metal surfaces converge and embed internally during deformation. This defect compromises structural integrity by creating stress concentration points that often lead to catastrophic failures. The following analysis details the root causes and resolution of folding defects encountered during production of 20CrMnTi transmission second shaft gears.

Defect Manifestation and Metallurgical Analysis

Post-carburization machining revealed circumferential defects near bore regions in 6% of production units. Metallographic examination showed:

  • Blunt termination morphology (vs. sharp crack propagation)
  • Inclusion bands within defect zones
  • Decarburization evidence in adjacent material

The defect formation energy follows the strain energy relationship:
$$ E_f = \int_0^{\varepsilon} \sigma_f d\varepsilon $$
where $\sigma_f$ represents flow stress and $\varepsilon$ effective strain.

Systematic Root Cause Analysis

Potential Cause Investigation Method Conclusion
Raw material defects Surface topology scanning Random distribution ≠ localized defect
Cutting-induced imperfections End-face metrology Shear-free sawing eliminated burrs/concavity
Metal flow abnormalities DEFORM 2D simulation Primary folding mechanism confirmed

Metal Flow Dynamics in Gear Forging

Finite element analysis revealed critical flow imbalances during final forging:

  • Velocity differential between web ($v_w$) and flash zone ($v_f$):
    $$ \Delta v = v_f – v_w \geq 8.2 \text{ mm/s} $$
  • Strain rate divergence at transition radius:
    $$ \dot{\varepsilon}_r = \frac{\partial v_r}{\partial r} $$

Simulation results demonstrated metal reflux patterns causing surface entrapment at the web-flash junction. This folding initiation occurs when:
$$ \frac{v_f}{v_w} > 1.6 $$

Die Modification Strategy

Geometric redesign addressed flow imbalances through:

Parameter Original (mm) Optimized (mm) Improvement
Transition radius R5 R8 60% increase
Flash land depth 3.0 6.2 107% increase
Web thickness 4.8 5.2 8.3% increase

The velocity gradient reduction achieved through radius modification follows:
$$ \nabla v_{new} = \nabla v_{old} \times \left( \frac{r_{old}}{r_{new}} \right)^{1.2} $$

Validation and Implementation

Post-modification simulation showed:

  • Velocity differential reduction: $\Delta v \leq 2.4 \text{ mm/s}$
  • Flow angle optimization: $\theta < 35^\circ$ (vs. original $52^\circ$)
  • Strain homogenity increase:
    $$ H_{\varepsilon} = 1 – \sqrt{\frac{\sum(\varepsilon_i – \bar{\varepsilon})^2}{n}} \geq 0.87 $$

Production verification demonstrated 100% elimination of folding defects, validating the gear forging process optimization. The solution reduced scrap rate from 6% to near-zero while maintaining dimensional specifications.

Technical Recommendations for Gear Forging

Preventative measures for similar components:

  1. Maintain radius-to-thickness ratio: $ R/t \geq 0.16 $
  2. Control metal velocity ratio: $ 0.8 \leq v_f/v_w \leq 1.3 $
  3. Implement pre-forging when volume distribution $ V_{web}/V_{flange} < 0.4 $

The folding prevention criterion can be generalized as:
$$ \Psi = \frac{R \cdot v_w}{t \cdot v_f} \geq 0.45 $$
where $\Psi$ represents the forging stability index.

This systematic approach to gear forging defect resolution demonstrates how targeted die modifications, guided by computational modeling, effectively eliminate folding while enhancing process robustness. The methodology provides a transferable framework for complex forging production optimization.

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